Exploded a belt today

cheeky24

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Hey guys just exploded a belt today not sure really what causedit as I wasn't really working it that hard it had no pulled threads and only had about 300 km on it any of u guys having belt issues
 

Dannyturbo

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I blew up my first one 100km after turbo install (1300 original km) going down a groomed trail, pulled a cord on the next one first day this year on the first hard pull( probably 500km on that belt), I will be doing an alignment check right away if that's good I will probably install a blow hole and/ or float the secondary, my clutches tend to get super hot especially pulling my fat arse up the hill


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fredw

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Not sure if it is a fluke on yours or not, but on my older 11 I had to put a 200thou shim in to push out secondary, it allied primary and secondary much better and no more belts went out, and ran much cooler overall..

a turbo will go threw belts quicker than n/a but still a 1000mile belt life is not out of line for it I found..

take me a look at your pri to secondary, it should look fairly straight with belt installed, if it looks like a bad dogleg you could use a alinment
 

oler1234

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Sometimes they just blow from stress and stretching... We ran dayco xtx belts on our turbo. That gates carbon fibre version would minimize belt stretch.
 

Caper11

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You didn't take the plastic spacer out of the primary did you??


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cheeky24

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One thing I did find was my weights for the pins had backed out about 3/16 and one was gouging putter clutch so relocktited and reinstalled got lucky there
 

slededjr

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Check alignment. Check both clutches to make sure nothing binding or stuck/sticking.
 
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